Here's what it looks like. There just isn't any more tension left in the elastic that runs across the top of the pocket.
I've also seen this pocket-sag on older Mercedes and BMW cars, as well as the "other" Swedish brand which shall remain nameless.
I'd think the way I repaired this is applicable to any car that uses this type of pocket. If you have a 'mesh' pocket, like the legendary Mercedes W123 cars, you'll have to take a slightly different approach, since the elastic is exposed and not hidden under fabric.
I'm just going to cut open the seams at either end of the top of the pocket, connect a new piece of elastic to the old one, pull it through, and sew it all back up.
This is the right side of the pocket. You can see the stitching that makes a little 'tunnel' flap that the elastic passes though, holding the pocket tight up against the seatback.
With my new 'ergonomic' seam ripper (cost $1 more than the standard model...), I cut the stitches at the end of the flap.
The pocket and the elastic were originally all sewn into a seam at the edge of the seatback. I'm just trying to undo enough to get at the end of the old elastic.
Here's the elastic on the right side of the pocket after I pulled some stitches out. About 18mm wide I'd guess.
I'm going to attach a long piece of new elastic to this, then cut the old one on the side where it attaches to the seam on the seat - leaving a couple inches (maybe 5cm...my brain's Imperial-to-metric converter is working today) to work with to attach the new piece to.
It's not pretty, but it's functional. I used 3 safety pins to hold the new piece (lower one) to the old piece.
Then I took a deep breath and cut the old piece.
Then I went to the other, uncut end, and pulled the old elastic through the little tunnel.
It worked! In fact, it took 2 seconds for the thing to pass through. And to think I was wondering it the pins would get hung up. Worked like a charm.
Here's our seat with the new elastic passed though the pocket.
As an aside: the elastic I used was 3/4 of an inch wide - it pretty much matched the width of the old piece exactly.
I cut the other side (left) and attached the new elastic to the short piece of the old elastic which was still sewn to the seat.
Then I pulled the other end of the elastic tight and fastened it to its respective old elastic end.
It took a few attempts to get it pulled up tight. I used small safety pins to hold the two ends of elastic together - I tried sewing them but it went nowhere fast. The thread just wouldn't hold together under tension. The pins aren't visible - they're tucked under the leather flap at the top of the pocket.
Last step was to resew the ends of the flap back together. In the picture you can see my new thread and the needle I used. You can also see the original stitching I pulled out (on the left).
I didn't want to just cut the old stitching since I figured it might eventually unravel over its whole length. So I ran my stitches over it to lock it down.
Here's one of the finished parts I did. You can see my stitches - they're a lighter color thread than the original. But note how I ran stitches over the original thread. Not the best sewing job, but it's functional and from a foot away, you'd never notice.
This is the finished pocket. Not perfect, but a lot better looking than it used to be (compare with the first picture above).
The bottom of the pocket is pretty stretched out from years of having stuff in it. But overall, not bad.
Now I need to find time to get the other seat out and repair it.
0 comments:
Post a Comment